My THP failed it's MOT on emissions today. The garage used the term "failed spectacularly" and said the emissions are at a level they'd expect to see from a dodgy remap. The only mods are an induction kit (the filter is clean and in perfect condition) and a resonator delete and back box. The car hasn't been running well for a while with hesitation, juddering and persistent pending fault codes for rich fuel mixture. It seems to bog down when pulling out of junctions followed by a noise similar to turbo flutter on occasion when it picks up again (the diverter valve diaphragm is intact and it appears to be functioning correctly). Fuel consumption has gone through the roof too. I've replaced the plugs and coils already, as well as the coolant temperature sensor but it's still running rich. My next port of call is the upstream lambda sensor and both map sensors in an effort to cure the issue. I replaced the temperature sensor as the gauge never reads more than a quarter of the way up but its still reading low. I'm presuming this will increase fuelling due to the engine running cooler but surely not to the extent that it has. Either way a new thermostat housing is also on the to do list in case the thermostat is stuck in the open position. A walnut blast is also on the cards as it's now done just over 30k so is probably in need of one.
Sorry for the long post but does anyone have any suggestions for anything else that could be causing the issues? I love the car when it works but at this point in time I'm wishing I'd bought something else.
Sorry for the long post but does anyone have any suggestions for anything else that could be causing the issues? I love the car when it works but at this point in time I'm wishing I'd bought something else.
Comment